well repair – part 2

In my previous post (part 1) I describe the temporary repair I made to the expansion tank pressure switch.  However the pipe/nipple connecting the pressure switch to the water manifold is badly rusted and seeping water and just a matter of time before it disintegrates.

I want the repair to proceed efficiently and so I researched how to removed broken nipples – Bob’s plumbing video (how to remove a broken pipe) was very helpful.  So prior to commencing the repair I bought and assembled all the tools and parts I would need – new pressure gauge; new pressure switch set for range 30psi to 50psi; 4″ long 0.25″ diameter brass pipe; an extractor kit for broken pipes; assortment of brushes to clean threads; rust penetrant oil; and my usual assortment of standby tools.  And then off to the well head.

Caution – following involves working with 240 volts and can result in serious injury or death and should not be undertaken by anyone not competent in this area.

I first switched off the power, then removed dome and pressure switch cover and photographed the wires so I could remember later which were connected to which.  With a tire gauge I measured the air pressure in the expansion tank – it was 45psi.  I opened a faucet and drained the water from the expansion tank.  Then I looked at the nipple and, as previously mentioned, it was in bad shape.

with the switch disassembled you can see the extent of rusting of the switch and nipple
with the switch disassembled you can see the extent of rusting of switch and nipple

After dowsing with rust penetrating oil I tried gently undoing the nipple from manifold and it turned for a bit and then broke away leaving some pipe in the hole.

some rusted pipe remaining in whole after unscrewing the nipple
some rusted pipe remaining in whole after unscrewing the nipple
you can see the rust and the small water hold and the little bit of thread which unscrewed
you can see the rust and small water hole and little bit of thread which unscrewed

With my nipple extractor the rest of the pipe in the hole appeared to disintegrate and I then cleaned the female threads with brass brushes.  While I was at it I also removed the broken water gauge.

the 2 cleaned holes - 1 for the nipple, 1 for the gauge, and the old gauge
the 2 cleaned holes – 1 for the nipple, 1 for the gauge, and the old gauge

And installed a new gauge and was disconcerted to see that somehow I had cracked the glass cover.  I used pipe thread sealant and connected up the  new pressure switch and pressure gauge.

the new parts in place and the expansion tank charged. I will try replace the cracked glass cover of the gauge soon.
the new parts in place and the expansion tank charged. I will try replace the cracked glass cover of the gauge

And then switched on the power and watched the gauge rise to 50psi and heard the switch click open and stop the pump.  Everything was working fine.  I checked the expansion tank pressure with my tire gauge and it was 45psi.  Mission accomplished.

 

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